Home About us Contact us Training Optimisation Services Protuner Educational PDFs Loop Signatures Case Histories
Michael Brown Control Engineering CC
Practical Process Control Training & Loop Optimisation
CONTROL LOOP CASE HISTORY 181
UNDERSTAND THE BASICS OF THE COMPONENTS IN THE LOOP
Many of the unresolved or even undiscovered problems I find on faulty or badly performing control loops are due to a lack of knowledge, or lack of logical thought on the part of both C&I (control and instrumentation) and process personnel.
I still find that the general prevailing “belief” in plants is that any control loop can be made to work well by tuning it. If the tuning doesn’t fix the problem the usual comment is that “tuning is a black art and we’ll just keep on fiddling with knobs until it comes right”. Eventually they give up and the operators make changes in manual or just leave it in manual all the time.
Loop optimisation is in fact only successful when the control objectives are fully understood, the process dynamics are established, and a thorough investigation is made of the loop to ascertain any faults and/or problems in the control strategy. Only when these things are done is one able to confidently apply scientific tuning to allow one to achieve the control objectives.
As many readers are aware from numerous articles I have published that generally the main problems in control loops are found in the final control element, which is usually a pneumatically actuated valve. In fact I can confidently say that at least 75 – 85% of control loop faults occur in the final control element equipment, i.e. valve, positioner and I/P converter.
Apart from this we do sometimes find problems in other loop components like the measuring system, and very often with incorrectly configured control blocks (mainly in PLC control systems).
Figure 1 is closed loop recording of the loop with the “as-found” tuning. It can be seen that the setpoint was coming from a cascade master controller, which was also interacting slightly with the flow loop, as it sometimes also cycled at the same frequency. However when the setpoint started moving higher the cycle stopped and the controller managed to get the flow to follow the setpoint reasonably well, although very slowly and seldom actually got to setpoint.
Figure 1.
How does one go about to try and solve a problem like this? It is certainly not by playing with the tuning parameters. One must first analyse the components of the loop which consist of the following:
1. Measuring transmitter.
2. Controller.
3. The operation of the actual process itself.
4. The control valve.
Normally to trouble-shoot the loop one performs a closed loop test (like the above mentioned one), and then an open loop (controller in manual) test where several step changes are made on the PD (controller output). These two tests if carried out properly will generally give one all the information required to identify any problems, and then, if they are not too severe, to apply scientific tuning.
Figure 2 is a portion of the open loop test that we performed on this flow control loop, and reveals the following information:
FIGURE 2
a) The PG (process gain which is the magnitude of the PV step size divided by the magnitude of the PD step size) is about 2.5 and this would suggest that the valve may be about 2 – 3 times oversized.
b) Based on the first 3 steps it looks like the valve has reasonable installed linearity.
c) Of extreme importance it can be seen that the flow PV drops to zero when the flow goes below 12%.
d) The response of the PV to step changes on the PD is very much in the form of a first order lag and is quite slow for a flow using a pneumatically operated control valve. This would indicate that a lag filter probably exists somewhere in front of the PV input to the controller. It could be on the transmitter or in the control system. It was in fact found that a 3 second filter was inserted in the control system. Filtering is another subject of which I have written about many times, and is generally not recommended or necessary.
One can now immediately understand why the loop was cycling in automatic when the setpoint was very low, as soon as the flow dropped below 12%, the PV dropped to zero, so the controller then opened up the PD to open up the valve to bring the flow up . Once the flow got back past the 12% and past the set point, the controller then tried shutting the valve to bring it down, which closed the PV down again and so it went on.
One must always ensure that the basics are correct. The first thing here to check on is what type of measurement technique was being used. In this case it was an orifice plate with a transmitter measuring the differential pressure across it. This type of measurement is one that goes back over several centuries, and is still commonly used. Any C&I practitioner will have studied the technology. There are many international standards dealing with it. However to my amazement I find that time and time again people are ignoring the basic rules, and seem to think that because these days we are using “smart” (computerised) transmitters that the basic rules can be ignored.
One of the general rules on differential head flow measurement particularly using orifice plates as the primary element is that they should never be used when the flow drops below 25%. In fact one of the standards actually recommends a lower limit of 33%. However over many years it has been accepted that for control purposes a lower limit of 25% is acceptable.
There are many reasons for the low limit, one of which is that the flow is proportional to the square root of the differential pressure, which means very tiny differential pressure values at low flows, but there are other factors including the fluidic behaviour at low flows. In certain cases on certain fluids low readings can be completely wrong, let alone very inaccurate.
To try and prevent use of the transmitters at very low flows most manufacturers of differential pressure transmitters have a low flow “cut-off” incorporated into the transmitter, which these days the user can set. This is the reason why in this case the transmitter was cutting off at 12%.
As can now be seen the problem here was incorrect flow measurement. No tuning can overcome the problem.